Canning Stock
Route Well 26
Project
It was reported
that Well 26
infrastructure
had been struck
by lightning and
burned to ground
level. The
windlass was
still intact and
it was still
possible to
retrieve good
water from the
well but very
unsafe to do so.
Track Care WA
decided to make
it a priority to
rebuild the well
to a condition
to make it safe
for public use.
Photos from
visitors showed
the well lining
timbers were
actually burned
below ground
level and it was
thought some
timbers lower
down were
falling in as a
result of tree
root activity.
Use was made of
sketches used by
the 1983 rebuild
team which were
based on
Alfred Canning’s
original
drawings.
Donations were
solicited and
sourcing of
materials and
manufacture of
components was
commenced in
April 2011.
While it would
be preferable to
use plastic look
alike sleepers
for longevity,
they proved too
expensive, so
Jarrah timber
was sourced for
the lining and
platform, and
pine logs for
the fencing and
troughing rails.
A busy bee was
held to cut
timbers to size
and shape to
minimise time at
the
well site.
The group of 11
vehicles, 5 with
trailers
carrying 3T of
materials left
for the CSR
on Tuesday 5
th
July 2011,
picked up a
submersible pump
in Newman and
arrived at the
well site on
Sunday 10
th
July 2011. Some
trailer damage
was
sustained
requiring track
side welding
repairs, and
extensive
snatching of
heavy trailers
over sandhills
made heavy
going.
Photo of Well 26
after lightning
destroyed the
upper timbers.
It was intended
to use the
‘airstrip track’
from Well 23
which runs NW
around
some lakes then
east to rejoin
the CSR just
north of Well
26. At our
request
some Rangers
from Parnngurr
Community
checked the
track the week
before
the party left
and
found
it impassable
due to deep
water across the
track.
Unfortunately,
the sandhills on
the CSR between
Well 23 and Well
26 were
formidable to
the loaded
trailers and
caused delays.
An advance party
had arrived at
the well 2 days
before and set
up a temporary
toilet and
commenced
removing the
loose and burnt
out timbers from
around
the well.
After arriving
midmorning on
the Sunday 10
th
July, volunteers
set to
installing a
trash pump into
the well which
pumped out water
and sand which
had found
its way into the
well. Then it
was hard work
pulling up
buckets of sand
and
water by hand.
Other volunteers
commenced
installing the
new sheet metal
troughing and
rails, then,
when it was safe
to work at the
top of the well,
replaced the top
3
layers of
sleepers, the
surrounding
platform, a
perimeter fence,
and reinstated
the old
windlass.
There was no
sign of the
whipping pole or
the two large
cast iron
pulleys so
this feature wa
s
not reinstated.
We had pre
arranged to meet
up with a group
of Rangers from
Parnngurr
Community who
arrived on
Monday.
The Rangers
attended to
business in the
area while the
volunteers
completed
the structures,
pumping out the
well 5 times to
flush the lower
levels, and
cleaned up the
Well 26 area.
Work was
completed in two
and a half days.
The well was
measured to be
making approx
4600L per hour
and CSR
travellers
were already
queuing to draw
the clear fresh
water.
Well 26
Restoration Team
July 2011